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Thursday, November 19, 2020
Diode Ring Magic
Tuesday, November 17, 2020
A Diode Ring Product Detector for the HA-600A? Problems.
I got the two diode, one transformer product detector working well, but with it a new problem arose: 455 kHz energy from the BFO was leaking past the product detector back into the S-meter/AGC circuitry. This showed up in the form of a constant S-3 reading when I switched to SSB/CW. This was annoying.
I figured the problem was that the only signal really being balanced out was the IF signal going into L1 of the product detector. I took another shot at putting the BFO signal into this port, with the IF signal going into the unbalanced potentiometer port. This did indeed take care of the BFO leakage S-meter problem, but once again the SSB did not sound great -- I think the old problem of simultaneous envelope and product detection returned.
This was obviously a port isolation problem. I remembered that the diode ring "doubly balanced" configuration has much better port isolation. So on Sunday morning I built one, first in LTSpice and then on the bench.
For the bench model I used some PC board pads out of Pete Juliano's $250,000 CNC machine. For the toroids I used two trifilar coils wound by Farhan's dedicated staff in Hyderabad. The diodes were sent to me by Jim W8NSA. So there was lots of soul in this new machine.
The circuit worked in LT Spice and at worked well when tested on my bench with my FeelTech (for the BFO) and HP8640B (for the IF signal) sig gens with my Rigol 'scope watching for the audio out.
But I ran into some problems when I popped the new board in there in place of the old product detector: The 455 kc BFO leakage problem is gone and the S-meter is where it should be, but...
-- I'm seeing a return of the old simultaneous envelope and product detection problem. SSB was sounding scratchy again and indeed, when I removed the BFO signal from the diode ring circuit I could hear SSB signals making it into the audio amplifiers. These signals sounded just like AM signals as heard through an envelope detector without a BFO.
-- The diode ring circuit also had a very bad effect on how the HA-600A worked in AM mode. It seemed like the new circuit was loading down the diode AM demodulator. SW broadcast signals sounded awful in the AM mode until I disconnected the IF input to the diode ring circuit (this input is NOT switched -- it is always connected, even in the AM mode).
So, for now, am back to using the two-diode, single transformer, singly balanced product detector with IF signal going to the balanced (L1) port and the BFO going in through the wiper of the 100 ohm pot.
Any suggestions on how to overcome the problems with the diode ring circuit?
Friday, November 13, 2020
How Does My Singly Balanced, Two-Diode, Single Transformer Product Detector Really Work?
As young James Clerk Maxwell used to say, "What's the go of it?" and "What's the particular go of it?"
I studied this circuit carefully when I was using it as a balanced modulator in my DSB rigs. I wrote up my conclusions in my book "SolderSmoke -- Global Adventures in Wireless Electronics."
BALANCED MODULATOR CONFIGURATION:
When I was using it as a balanced modulator, I had the RF "carrier" signal going into L1. This RF signal was 7 dbm, enough to switch the diodes on at voltage peaks. With the "center tap" of L2/L3 grounded for RF, this meant that when the "top" of L2 is negative, the "bottom" of L3 is positive. In this situation BOTH D1 and D2 will turn on and conduct.
When the top of L2 is positive, the bottom of L3 is negative and neither of the diodes is on. Neither conducts.
So we have the RF signal turning the diodes on and off at the frequency of the RF signal.
Audio from the microphone and mic amplifier is sent into the center tap connecting L2 and L3. The level of this audio is kept low, below the point where is could turn on the diodes. The center tap IS grounded for RF by the .1uF capacitor, but it is NOT grounded for AF. That is key to understanding this circuit.
In essence by turning the two diodes on and off at the rate of the RF signal, the audio signal is facing severe non-linearity through the diodes. We could say it is alternately being multiplied by 1 and 0. This non-linearity is what is required for mixing. We therefor get sum and difference products: Sidebands. At this point, Double Sideband.
The way the transformer is set up means the RF carrier signal is balanced out: Even when the two diodes conduct, the top of R1 and the bottom of R2 are of equal and opposite polarity, so there is no carrier signal at the junction of R1 and R2 (they are actually a 100 ohm variable resistor that can be adjusted to make SURE they balance out). So the carrier is suppressed and all that remains are the sidebands: Suppressed Carrier Double Sideband.
PRODUCT DETECTOR CONFIGURATION:
What happens when we use this circuit as a product detector in a receiver? Let's assume we are working with a 455 kc IF. If you run a 454 kc 7 dbm BFO signal into L1, it will turn the diodes on and off as described above. But you will NOT be able to put the 455 kc IF signal into the center tap of L2/L3 -- that center tap is GROUNDED for 455 kc. So you will have to run your IF signal into the resistors, and take the audio output from the center tap of L2/L3. This works. I tried it in my HA-600A. But there is a problem: Envelope detection.
In this arrangement, we are balancing out NOT the 455 kc IF signal, but instead we are balancing out the BFO. We don't really NEED to balance out the BFO -- it can easily be knocked down in the audio amplifiers, and IT is not responsible for the problematic envelope detection. We DO need to balance out the IF signal, because if that gets through we can get simultaneous "envelope detection" and product detection. And believe me, that does not sound good.
So I tried putting the IF signal into L1, and the BFO signal into the resistors (as shown above). I took the audio from the junction of L2/L3. This seemed work better, with envelope detection greatly reduced.
BUT WHAT'S THE GO OF IT?
But how is this circuit mixing in this configuration? The strong BFO signal is still controlling the diodes, BUT, with the BFO signal coming in through the resistors, when the top of R1 is positive the bottom of R2 is ALSO positive. In this situation D1 will conduct but D2 will not. The IF signal is facing a big non-linearity. This will result in sum and difference frequencies. The difference frequency will be audio. But with D1 and D2 turning on and off in a very different way than we saw in the balanced modulator, how does the mixing happen?
I think the answer comes from the summer 1999 issue of SPRAT, the amazing journal of the G-QRP club. Leon Williams, VK2DOB wrote an article entitled "CMOS Mixer Experiments."
Here is Leon's 74HC4066 circuit:
I think those two gates (3,4,5 and 1,2, 13) are the functional equivalent equivalent of the two diodes in our product detector. In Leon's scheme the VFO is supplying signals of opposite polarity. Ours is providing only one signal, but the fact that the diodes are reversed means that they act just like the gates in Leon's circuit. The transformer is almost identical to the one we use in the product detector.
Let's look at the output from Leon's circuit:
Monday, November 9, 2020
Improving the Product Detector in the Lafayette HA-600A
Steve N8NM built the HA-600A product detector both in LTSpice and in the real world. It worked fine in both versions. Steve even put the product detector into his S-38 receiver -- he reported it worked well there.
I too built the thing in LTSpice. Then I went and rebuilt the circuit on a piece of PC board. I connected the new circuit to the HA-600A, using my external FeelTech sig generator as the BFO. IT STILL SOUNDED BAD ON SSB.
At this point I started Googling through the literature. I found a promising article by Robert Sherwood in December 1977 issue of Ham Radio magazine entitled "Present Day Receivers -- Problems and Cures." Sherwood wrote:
"Another area that could use additional work is the product detector. As the name implies, its output should be the product of the two input signals. If BFO injection is removed, output should go to zero. If this is not the case, as in the Heath HW series, envelope detection is also occurring, which causes audio distortion."
I checked my circuit. When I removed the BFO signal from the product detector, envelope detection continued. In fact, with the receiver in SSB mode, and with the BFO disconnected, I could listen to the music of WRMI shortwave. It seemed that Sherwood was explaining well the problem I was having: Simultaneous envelope and product detection was making SSB sound very bad in my receiver. What I was hearing just seemed to SOUND like what you'd get with a mixture of product and envelope detection: "scratchy" sounding SSB. This also seemed to explain why SSB would sound fine when using the diode detector with loosely coupled BFO energy -- in that case it would be envelope detection only, with no ugly mixture of both kinds of detection.
Finally, I needed to find a way to use the BFO in the HA-600A with the new product detector. Obviously I needed more BFO signal -- I needed about 7 dbm, enough to turn on the diodes. I converted the outboard product detector board into a simple amplifier and put it between the HA-600A BFO and the BFO input port of the new product detector. This works fine.
A few issues remain:
1) The output from the HA-600A BFO through the above BFO amp (and across the 50 ohm resistor) is NOT a pretty 455 kc sine wave. But the peaks of the distorted wave appear to be enough to turn on the diodes, and when I look at the voltages across each diode (on my two channel 'scope) I see mirror images -- one is on when the other is off. Is this good enough?
2) Moving the BFO input from L1 to the junction of the two 50 ohm resistors (that is actually a 100 ohm pot) has big implications for how this mixer works. With the BFO energy going through the toroid, BOTH diodes are being alternately turned on and turned off. But both are on, and then BOTH are off. With the BFO energy going in through the other side, one diode turns on when the other is off. I think the mixing result is the same, with AF coming out of the output port, but the way the mixer works in this configuration is very different. Does this sound right?
Saturday, October 31, 2020
SolderSmoke Podcast #226 The U.S. Election, Solar Cycle, uSDX, Hermes, HP8640B, SGC 600 Sig Gen, HA-600A, Mailbag
SolderSmoke Podcast # 226
http://soldersmoke.com/soldersmoke226.mp3
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About the U.S. election
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Mars: Setting early, will have to shift to evening observation. Weather has been poor.
Sunspot Cycle 25 is underway -- SFI 78, SN 32
The Gliessberg cycle
Pete's Bench: #49, #50, uSDX, Hermes Lite
Bill's Bench: HP8640B, Global Specialties Corp 6000 counter, Lafayette HA600A.
MAILBAG:
Peter VK2EMU Sent me copy of 1947 Handbook. Thanks Peter
Brad W1BCC Spotted 10 S-38s for 80 bucks on Craig’s list. What’s going on here?
Dale K9NN sent both Pete and I care packages with very cool part, including DG Mosfets
Stuart ZL2TW sent me Les Moxon’s Antenna Book. TRGHS. Moxon will be back!
Alvin N5VZH got his receive converter with a little Tribal Knowledge from SS.
GM4OOU The Bitsy DSB rig from Scotland
Peter VK3YE DSBto DC incompatibility SOLVED
Paul VK3HN's Digital SWR and Power Meter and Low band AM TX VFO/Controller FB Videos.
VK2BLQ alerts us to article about Jac Holzman of Elektra Records.
AA0ZZ great message on assembler language and writing software the hard way.
Thursday, October 15, 2020
Too Simple? Deficiency of the Lafayette HA-600A Product Detector?
I've been having a lot of fun with the Lafayette HA-600A receiver that I picked up earlier this month. Adding to the mirth, I noticed that on SSB, the signals sound a bit scratchy, a bit distorted, not-quite-right. (I'm not being facetious; this is an interesting problem and it might give me a chance to actually improve a piece of gear that I -- as a teenager -- had been afraid to work on.)
Before digging into the circuitry, I engaged in some front panel troubleshooting: I switched to AM and tuned in a strong local AM broadcast signal. It sounded great -- it had no sign of the distortion I was hearing on SSB. This was an important hint -- the only difference between the circuitry used on AM and the circuitry used on SSB is the detector and the BFO. In the AM mode a simple diode detector is used. In SSB a product detector and BFO is used. The BFO sounded fine and looked good on the scope. This caused me to focus on the product detector as the culprit.
Check out the schematic above. Tr-5 is the product detector. It is really, really simple. (See Einstein quote below.) It is a single-transistor mixer with BFO energy going into the base and IF energy going into the emitter. Output is taken from the collector and sent to the audio amplifiers. (A complete schematic for the receiver can be seen here: https://nvhrbiblio.nl/schema/Lafayette_HA600A.pdf )
I had never before seen a product detector like this. One such detector is described in Experimental Methods for RF Design (page 5.3) but the authors devoted just one paragraph to the circuity, noting that, "We have not performed careful measurement on this mixer." The lack of enthusiasm is palpable, and probably justified.
A Google search shows there is not a lot of literature on single BJT product detectors. There is a good 1968 article in Ham Radio Magazine: http://marc.retronik.fr/AmateurRadio/SSB/Single-Sideband_Detectors_%5BHAM-Radio_1968_8p%5D.pdf It describes a somewhat different circuit used in the Gonset Sidewinder. The author notes that this circuit has "not been popular."
To test my suspicion that the product detector is the problem, I set up a little experiment. I loosely coupled the output of a signal generator to the IF circuitry of the HA-600A. I put the sign gen exactly on the frequency of the BFO. Then, I switched the receiver to AM, turning off the BFO and putting the AM diode detector to work. I was able to tune in the SSB signals without the kind of distortion I had heard when using the product detector.
So what do you folks think? Is the product detector the culprit? Or could the problem be in the AGC? Should I start plotting a change in the detector circuitry? Might a diode ring work better?
Thursday, October 8, 2020
HA-600A Gets a New Coat of Paint -- After Almost 50 years!
Tuesday, October 6, 2020
TRGHS -- My First SW Receiver Offered FREE for Pickup -- The Lafayette HA-600A (Looking for Globe VFO Deluxe)